ArashB
04-28-2017, 04:52 PM
Extremely loud boom and jerk when shifting into drive or reverse!
Greeting, I recently cleaned the throttle body on my Previa (~240km/150miles) but after reinstalling it, shifting has been a nightmare at stand still... but the van still performs really great otherwise. This condition gets worse when the engine is warm\hot.
Also after going through drive and reverse a number of time, what sounds like a detention, reduces greatly.
I even installed a different throttle body but still have the same problem.
After much researching Ive come to a few conclusions.
1. Vacuum leak at the throttle body (I used the old gasket and added a bit of sealer the second time around) or the large intake hose may not be clamped hard enough.
(To test this I will be buying a propane extension hose [and fire extinguisher] and see it seeps in to change idle sound)
2. One of the sensors locking clip broke (light coloured) and it may not be pushing in all the way or I may have damaged the wires connecting one of the adapter. (can i disconnect any to see if the connects are in tact?)
3. I may have pulled the "kick down" throttle cable too hard initially when I was amateurishly trying to get the throttle body off its screw bolts. It is currently adjusted with the 1mm spacing.
4. I currently have the battery disconnected (over a few hours) incase the old idle rpm settings in the ecu need to be reset.
My father should be coming to town soon so that I could connect a scanner and get some readings to help hopefully.
Thanks for reading.
p.s. I read this on the Zen Adventures site... maybe it could help diagnose my problem.
http://i.imgur.com/VbnNLHW.jpg
(http://i.imgur.com/VbnNLHW.jpg)
Greeting, I recently cleaned the throttle body on my Previa (~240km/150miles) but after reinstalling it, shifting has been a nightmare at stand still... but the van still performs really great otherwise. This condition gets worse when the engine is warm\hot.
Also after going through drive and reverse a number of time, what sounds like a detention, reduces greatly.
I even installed a different throttle body but still have the same problem.
After much researching Ive come to a few conclusions.
1. Vacuum leak at the throttle body (I used the old gasket and added a bit of sealer the second time around) or the large intake hose may not be clamped hard enough.
(To test this I will be buying a propane extension hose [and fire extinguisher] and see it seeps in to change idle sound)
2. One of the sensors locking clip broke (light coloured) and it may not be pushing in all the way or I may have damaged the wires connecting one of the adapter. (can i disconnect any to see if the connects are in tact?)
3. I may have pulled the "kick down" throttle cable too hard initially when I was amateurishly trying to get the throttle body off its screw bolts. It is currently adjusted with the 1mm spacing.
4. I currently have the battery disconnected (over a few hours) incase the old idle rpm settings in the ecu need to be reset.
My father should be coming to town soon so that I could connect a scanner and get some readings to help hopefully.
Thanks for reading.
p.s. I read this on the Zen Adventures site... maybe it could help diagnose my problem.
http://i.imgur.com/VbnNLHW.jpg
(http://i.imgur.com/VbnNLHW.jpg)